A failure of any major
component meant starting over. Some
day’s one of us would run six of our 8 hrs. We had a fuel line connected to the
aircraft so it was not necessary to have a fuel truck to refuel.
We had several incidents
happen. I can only remember a few of the
important ones. On one occasion, I was running the aircraft and Bill Shisler
was sitting in. It was at night and we were churning away at high power when
suddenly without warning the engine quit. To go from extremely high noise level
to nothing is as startling as a sudden
noise.
To make matters worse, the
aircraft filled with smoke. We were
making a rapid departure, Bill was ahead
of me, I was trying to shut things off. We had a battery secured to the floor
just inside the cabin door, Bill fell over the battery and I fell over Bill,
and we both fell out of the aircraft. No injuries; the engine failure was
caused by a sheared accessory drive gear. That shuts off everything instantly.
The engine problem did not
affect our test, since we were not testing the engine, it was government
furnished, and was a continuing problem throughout the life of the HUP
aircraft. It was originally 550 HP but was derated to 475 HP.
We had periodic tear down
inspections. Transmissions were removed,
and inspected along with rotor hubs, and other components. During one of the
inspections a hairline crack was found in a web, which was part of the aft
transmission case.
Engineering labored over this
problem for some time, it could mean a start over if replaced. A decision was
made to bond four very small wires across the crack and connect four lights in the cockpit so that if the
lights started to go out it could mean the crack was progressing.
If this happened we should shut down immediately.
We were running again and watching the lights. It wasn’t long and one light
blinked a few times and out. We shut
down immediately. After careful consideration Engineering decided that one
light out wasn’t all that important so go ahead and run. This continued every time another light went
out.
It became something of a joke
with some of us. We finished the 500 hours, tore down the transmission, the
crack had not progressed even the wires were in tact.
Another incident on the HRP
tie down. I don’t remember the test we
were
running but I came in on day
shift to take over running from Bill Shisler, he had just shut down. I got in
the seat and fired it up. I engaged the rotor, brought it up to power, and
suddenly I saw a long piece of rope sucked up into the forward rotor followed by a large tarp. It wrapped
itself around one of the rotor blades and created an unbelievable shake.
I was thrown out of the pilot
seat onto the floor of the cockpit. The only thing I could get to was the
mixture control, and I was able to pull it to cutoff. All the tie down cables were stretched, I was
lucky it stayed in the cradle.
The one rotor blade was
destroyed, due to a bent spar. I wasn’t found at fault since I didn’t stow the
tarp under the aircraft.
Charles Kessler is a retired flight test engineer for
Boeing’s Vertol helicopter division (formerly Piasecki Helicopter Co.). He
joined Piesecki in 1947, in the company’s fourth year, and retired from Boeing
in 1983. During his 37-year career he took part in the testing of prototypes
and alterations of such models as the CH-47 Chinook and Sea Knight, the H-16,
HRP-2, and the V-107. He taught the stability augmentation system to the German
Luftwaffe. He has written about his experience in a blog called “Early
Helicopter Years,” which can be found at http://helicopterstory.blogspot.com/.
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